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2011-07-27 Set Agenda w/Attachments
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2011-07-27 Set Agenda w/Attachments
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7/27/2011 4:20:29 PM
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� $ Bergerson - Caswell Inc. <br /> :: <br /> .. � <br /> � `�� ° �' " = 5115 Industrial Street <br /> 4 � "" � Maple Plain, MN 55359 <br /> BER SON (763) 479-3121 Fax: (763) 479-2183 <br /> INGORPORATED <br /> July 22, 2011 <br /> CITY OF CENTERVILLE BONESTROO, INC <br /> 1880 Main Street Mark Statz <br /> Centerville, MN 55038-9794 2335 Hwy 36 West <br /> St Paul, MN 55113 <br /> RE: CITY OF CENTERVILLE Downtown Strom Water Reclamation Project, Phase i <br /> CHANGE ORDER REQUEST UPDATED to Contract B- Vertical Steel Casing for wet well <br /> BERGERSON CASWELL INC is performing Contract B of the referenced project above, and we were asked <br /> to provide a cost to the city for installing the wiring & electrical service to the newly moved garage at <br /> the project location (park). With this new location for the service and controls and the finalized location <br /> of the transformer, there is also an additional cost due for the longer run between the Xcel Transformer , <br /> and service meter as well as the additional length between the wet well and the new bldg. <br /> We met at site on Tuesday July 28, and discussed these changes and discussed the location of the power l i <br /> transformer. We also discussed removing the power disconnect at the well head (100 Amp), the �� <br /> handhole for pulling the feeder wires, and changing the size of the control transformer. Below I have � <br /> broken down these items and their costs. ! <br /> � <br /> i <br /> DEDUCT: 100 Amp disconnect and post at wet wellhead ! <br /> HANDHOLE � <br /> 1 KVA 480/240/120 Control transformer � <br /> i <br /> ADD: Wire and conduit to feed sub anel in bld will be wired on inside of the bld � <br /> P 6 � g) <br /> 15 KVA 480/240/120 power transformer <br /> 75' additional service entrance (2"C- 3#3/0, 1#4G) <br /> 60' additional service to wet well (2"C- 3#2, 1#4G) <br /> 60' additional control wires to wet well (3/4"C-1-2/C#14 SHLD) <br /> Additional hand digging required <br /> ***** Changes to meet electrical inspector add 200Amp 16 circuit 460/277 volt panel board <br /> With 3 pole breaker to feed VFD <br /> 1-60 amp pole to feed transformer and rearrange previously installed items <br /> CHANGE IN CC�NTRACT COST: ADD $8,380.00 <br /> If you have any questions on this change order request, or require additional information, please do not <br /> hesitate to contact us at (763) 479-3121. Keep us updated as to the status of this request thank you. <br /> Sincerely, <br /> BERGERSON CASWELL INC. Tim Berquam Project Manager <br /> Bergerson - Caswell Inc. <br /> 5115 Industrial Street • Maple Plain, MN 55359 <br /> Telephone: 763 - 479 - 3121 Fax: 763 - 479 - 2183 E-Mail: info@Ber,gersonCaswelLcom /� <br /> Equal Opportunity Employer/Contractor <br />
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