My WebLink
|
Help
|
About
|
Sign Out
Home
2001_0813_packet
Roseville
>
City Council
>
City Council Meeting Packets
>
2001
>
2001_0813_packet
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
10/3/2011 11:55:31 AM
Creation date
10/3/2011 11:40:49 AM
Metadata
Jump to thumbnail
< previous set
next set >
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
292
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
Emission Test Report <br /> .1VI 'VGA-208 <br /> Section 3 <br /> Revision: 0 <br /> - Date: September 30, 1999 <br /> Page 3 of 33 <br /> of non-simultaneous testing is that results obtained from the inlet during Run 4 <br /> are somewhat larger than the outlet results. <br /> • During the last two runs of regular testing (Runs 8 and 9),no M26A trains were <br /> used for sample collection at the outlet in order to conserve usable water-cooled <br /> probes. Particulate matter for these runs was collected on the metals train. <br /> Particulate matter results were not compromised by using a different train sample <br /> collection, however, no HC1 samples could be collected as a result. <br /> Some trains at the scrubber inlet location (Run 1 M.26A train Run 2 M29 train <br /> Run 2 M23 train Run 3 M.26 A train and Run 5 M23 train) did not pass final leak <br /> check from the nozzle, but did pass from the sample transfer line. This appeared <br /> to be caused by extreme temperatures loosening the nozzle-to-probe liner <br /> connection. Since 02, CO„ and moisture results were nearly identical for all <br /> 2 Y <br /> trains within a given run, results from these trains appear to be uncompromised <br /> a <br /> and representative of stack conditions. <br /> The PCDDIPCDF outlet trains for Runs 5 and 10 did not pass final leak check. These <br /> results are considered to be unusable and are therefore not reported. <br /> Thermocouples <br /> During Run 1, the probe thermocouple on the PCDDIPCDF train at the scrubber inlet <br /> location shorted out. This was replaced after the end of the run with the result that no <br /> probe temperature data was available for the second half of the run. However, based on <br /> �r <br /> x:. stack temperature and filter box temperature, this is not expected to have affected results. <br /> During Run 3, the XAD thermocouple on the PCDDIPCDF train started to fail, giving <br /> '::.:.. high temperature readings in spite of frequent applications of ice. It was replaced during <br /> port change and readings thereafter were well within method requirements. Data were not <br /> temperatures <br /> affected, since the high temperature readings were not a reflection of actual tem <br /> ..... g p g p <br /> thought to have been experienced at the XAD inlet. <br /> f <br /> Sample Recovery <br /> The recovery and QA rinses of the Run 1 PCDDIPCDF inlet and outlet sampling <br /> trains were not collected according to the test plan (see analysismemo in Appendix A). <br /> The recovery rinses for the semivolatile front-half (PMD/F4MF FH) filet were <br /> inadvertently placed into the SV FH inlet sample bottles. This was easily corrected by <br /> analyzing the recovery rinses labeled for the inlet with the outlet train samples and <br /> designating a new number for the inlet train rinses to prevent mix up during analysis. The <br /> r QA rinse from the PCDDIPCDF front-half outlet was inadvertently laced into the inlet <br /> MM-AMaa931-09-03 Slwo <br /> L <br />
The URL can be used to link to this page
Your browser does not support the video tag.