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<br />. - . <br /> . <br />. Mr. Dwayne Stafford <br />.. July 9, 1997 <br /> Page 2 <br />. the work. With "test and seal", a combination packerltelevision unit is pulled to each joint. The <br /> packer is inflated to isolate the joint and air pressure is applied to 'test" the joint. If the joint fails <br /> to hold air pressure, a grout sealer is injected into the joint and allowed to cure. After curing, the <br />. joint is retested until it passes an air test. Then the packer unit is moved to the next joint. With the <br /> difficult access, it may not be possible to do a test and seal program, but a flexible liner may be <br /> appropriate as an alternative. The cost of lining a pipe may be two or more times that of testing <br />. and sealing in normal cases. However, in this situation with access issues complicated we would <br /> anticipate that the costs will be closer together. Preliminary estimates suggest that the cost to <br /> slipline the 1,700 feet of pipe in this area may be about $120,000. <br />. Flow records are not available to measure the amount of Infiltration and Inflow (Ill) in this line but <br /> it is estimated that the joint leaks and leaking manholes contribute about 2.5 million gallons of flow <br /> per year to the line. During periods of higher ground water levels the flow rates may be somewhat <br />. higher. <br /> Valentine Park Easement <br />. This area includes approximately 2,255 feet of 15 inch RCP, 1,775 feet of 12 inch RCP, 614 feet <br /> of 12 inch vitrified clay pipe (VCP), 300 feet of 8 inch VCP, and 23 manholes. <br />'e The pipe structure appeared to be sound in the area between County Road E-2 and the railroad <br /> tracks. The condition was fair to poor in the north segment from Old Highway 10 to the lift station. <br />. Where the structure was good, there were numerous leaking joints and joints with mineral deposits. <br /> It appears that much of the sewer in this area was installed below the normal groundwater to level <br /> so infiltration will be in continuous problem throughout the year. Only 3 manholes were noted as <br />. leaking but in consideration of the groundwater conditions, additional manhole leakage is probably <br /> occurring. <br />. In the northern section where the structure was poor, there were significantly fewer leaks observed <br /> but there was heavy root intrusion and some significantly cracked pipe. The roots prevented <br /> complete viewing of the segments so there may be additional defects that were not observed. <br />. In the southern section a test and seal program would be appropriate, but access is also a problem <br /> so insertion of a flexible liner will be considered as a viable option. As previously described, the <br />. cost of sliplining may be reasonable in comparison to test and seal due to site conditions. In the <br /> northern section the sliplining would be appropriate to correct the pipe cracking and root intrusion <br /> problems. Using the same unit cost as previously stated, the estimate for sliplining both the <br />. northern and southern segments in this area would be about $340,000. <br /> The southern section of the area showed some potential for continuous III at an estimated rate of <br />I about 2.4 million gallons per year. During periods of more severe groundwater presence, the rate <br /> may be higher. <br />.. In the northern section the sliplining is intended to improve structural conditions and reduce <br /> maintenance needs, the I{I reduction benefit will probably be minimal. <br /> Howard R. Green Company <br />. CONSULTING ENGINEERS <br />